It was a good memory when I came to realize that the factory stator output is rated at only 1.5 amps. and everyone has had to deal with it, in their own way, some have sent the stator out to be rewound to 12 volts, and others have attached small alternators, I have been looking at all of these ideas, for the past year,
a while back I was going through some old stators off of some 4wheelers and snowmachines that were laying around, and came across one off of a 2001 Polaris sportsman 500, (4.528")and it was close to the same width as the 084 stator (4.642)" across, and that got me thinking a little bit. the Polaris stator being only .114" narrower, it could work.
The Polaris stator is rated at 250 watts from the factory ( if my calculation is correct that should equal around 20 amps.)
with a spare 084 stator, I took off the mounting plate, to see what it would take to fit it to the Polaris stator. nothing was really looking good, if I milled it flat and to fit, there just was not enough meat left to attach the new stator to it. the only other option I seen was to make my own custom mounting bracket/spacer to attach the stator to the timing gear cover.
So with that thought, I went to visit with my friend who owns a lathe and milling machine, and told him of my dilemma.
with not having a specific design in mind, and trying copy to some extent the original backing plate. we came up with the first design. without modifying the Polaris stator, and it recessed into the bracket as far as I dared. it was sitting still to high.
then we started looking at the casting on the inside of the starter pulley, with the rounded inside corners. it was not letting the stator sit down far enough. so we put it in the lathe and trued it up. you want to be careful with this, it appears to be thick, after trueing it to the base of the stator, the edge thickness is measuring .1530" or 3.88 mm. so making the starter pulley deeper was not a option. but it needed the inside cone, and the outside corner to be squared up for this style of stator.
after putting it on the motor, to see what the fit would be, it was still sitting out almost 3/8" to far.
I was getting a little frustrated, more with the fact, that I had just wasted 6-7 hours of my friends time, sure both of use learned a few new tricks to make the first bracket, to make a bracket from scratch, and to match 2 items together that were not machined to go together, was a fun challenge.
The only option left that i could see was to change up the way the stator mounts to the face plate, instead of using a mounting bracket, all i needed was spacer, to keep everything in alignment.
so the piece of aluminum that was 4"x 4"x 3/4", shrunk down to a round disc 2.5" on the outside, with a 1.67" hole inside, and .5" thick. and ended up with 3 separate sized steps on the outside, to keep things centered.
I ended up attaching the stator directly to the face plate. as you can see the mounting holes on the stator are very close to the seal. not much wiggle room. and with only being able to line up one of the 3 holes, to one of 4 bosses on the face plate, there just is not a lot of meat for the other 2 bolt threads.
so I made up a backing plate so the cap screws would have almost 3/8" or more of thread to hold it in place.
Also I ended up cutting out some of the plastic molding so it would sit down another 1/8 of an inch. Which has brought the original solder joints very close to the face plate.
this was so much simpler than the mounting bracket that was made the day before.
if my measurements are correct, I have a gap of .2640" between the top of the stator and the inside bottom of the starter pulley, more than enough room to solder the 2 wires and not have to worry about any clearance issues.
the height of the 084 stator from the face plate to the top of the stator is 1.4710", and the finished height of the polaris stator is 1.5050" with a height difference of .0340, if I bend over the solder connections that are on top of the Polaris stator, it will lower the overall height to almost 1/8" lower than the stock 084 stator.
things are looking good
I still might look at soldering them back on the bottom of the stator, just would need to see what I will need for clearance so the connection don't short out, on the face plate.
also I need to mill down the 4 existing bosses, where the original stator was mounted, at the moment there is maybe 1/16" of clearance.
For a voltage regulator, I will be using the one that Polaris made for this stator model.
on the starter pulley, we cut off the pull cord ears to start with, and that way we could keep the alignment true. but we found out also that the casting ring where the shaft comes out, is true also. and there was enough there, that the lathe jaws had a solid grip to make the cuts also.
still have a little more to do on this motor before starting it up and seeing if this all works.
but I am having fun trying different approach to the low voltage problem.
please let me know if I might be missing something on this modification.
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